Here's why the pilot of this stricken F-4D returned to base safely without his backseater

Here’s why the pilot of this stricken F-4D returned to base safely without his backseater

By Dario Leone
Aug 27 2018
Share this article

“My sensation was that the aircraft as out of control and I ordered Kenny to eject which he did. Instinctively, I took the stick and throttles in hand and to my amazement, the aircraft was flyable,” Ray Battle, F-4D pilot

On Nov. 18, 1968, an F-4D #66-0249 belonging to 433rd TFS, Ubon RTAB, Thailand, was Stricken by 37mm Anti-Aircraft fire that rendered the Phantom uncontrollable. Pilot Major Ben “Ray” Battle ordered his weapons system officer (WSO) 1Lt Robert “Kenny” Boone to eject.

After the ejection, the aircraft became controllable and Major Boone made a gear up landing at Ubon.

Battle survived the landing and Boone was rescued unhurt from the Laotian jungle.

Ray Battle recalls.

“Kenny Boone and I were flying a fast mover FAC mission along the Ho Chi Min trail in Laos. It was an orientation ride for Kenny as he was newly assigned to my unit. We were at 4000 feet and Kenny was flying the airplane when I heard an explosion, the aircraft shuddered and the front windscreen was covered in what turned out to be hydraulic fluid. My sensation was that the aircraft as out of control and I ordered Kenny to eject which he did. Instinctively, I took the stick and throttles in hand and to my amazement, the aircraft was flyable. I called for help for Kenny and headed back for Thailand where we were stationed. I was given the option of ejecting or landing gear up as the landing gear would not come down. I elected to land gear up and catch the runway wire with my tailhook.. I have 150 aircraft carrier landings and thought I could easily make an arrested landing on the runway. I pulled the power off just as I touched down and the aircraft settled onto the wire cutting it. The aircraft slid down the runway and veered off to the right before fish-hooking to the right and stopping. It caught on fire and I jumped out safely. As you know Kenny was recovered after spending a nervous night hanging in a tree in Laos. In retrospect, my ordering Kenny to eject was a mistake which I have always regretted. I felt at the time I was saving his life and I intended to eject after he did. We both survived the incident for which I am grateful.”

Here's why the pilot of this stricken F-4D returned to base safely without his backseater

As reported by Sierra Hotel Aeronautics, F-4D #66-0249 was eventually repaired, needing a new nose cone, some paint and a new seat for the guy in back. She was returned to service two years later in February of 1970, and went on to enjoy a long career. Sadly Ol’ #249 saw her end with a plunge in the Florida Gulf, flying out of Tyndall AFB in 1985.

Photo credit: U.S. Air Force


Share this article

Dario Leone

Dario Leone

Dario Leone is an aviation, defense and military writer. He is the Founder and Editor of “The Aviation Geek Club” one of the world’s most read military aviation blogs. His writing has appeared in The National Interest and other news media. He has reported from Europe and flown Super Puma and Cougar helicopters with the Swiss Air Force.

Leave a comment

This site uses Akismet to reduce spam. Learn how your comment data is processed.

Share this article


Share this article
Share this article

Always up to date! News and offers delivered directly to you!

Get the best aviation news, stories and features from The Aviation Geek Club in our newsletter, delivered straight to your inbox.



    Share this article
    Back to top
    My Agile Privacy
    This website uses technical and profiling cookies. Clicking on "Accept" authorises all profiling cookies. Clicking on "Refuse" or the X will refuse all profiling cookies. By clicking on "Customise" you can select which profiling cookies to activate.
    Warning: some page functionalities could not work due to your privacy choices